The Thread Spread

-GP760 Value Added-

Very Revvy
The Question - **This letter is from the same person I corresponded with in the Raider Sport Ports article.**
 
Rick Hi What's up, It's been awhile since I talked to you last. I just finished putting my motor back together, but before I did I snapped a few pictures for you to look at. Notice on picture 1, how the front steel liner is cut flush with the aluminum. This was done by Group K when they bored the cylinders. Picture 2 shows how the back liner is matched with the upper case. Picture 3 shows the shape of the exhaust port that I sent to you a couple months ago. Picture 3 shows how the cylinder matches up with the exhaust manifold. I am planning on dropping the engine into the hull this afternoon and probably breaking it in tomorrow.
 
Craig
The Response - It looks like some fine work there - nice pictures too [Sorry I can't put up all the pictures I get - Rick]. I appreciate the update. Case matching is always a good idea. Its benefits may be marginal but every little bit helps and it certainly doesn't hurt. Over the winter I rebuilt my GP760 motor too. I decided not to part with the $600+ for an after market exhaust pipe so I concentrated on making the motor more efficient. When I pulled off the head it was easy to see how the factory achieved the staggered compression, the whole combustion chamber is recessed a bit on the rear cylinders head. The static compression of that cylinder would read about 5 to 7 lb. less than the front one. I CCed the head on the motor with the pistons installed to establish the uncorrected compression ratio (UCCR). It turns out the engine is shipped with an UCCR of 12.28 :1 (up front). That's pretty good for running low octane pump gas (86 whenever possible). The tub head combustion chamber design and over cooling help to keep
everything in check. The squish area of the head was so thick I think it was virtually useless. When measured, the squish was determined as being 2.46 mm thick on the front cylinder and 2.84 mm on the rear cylinder - ugh. I decided to base all design changes off the front cylinder because I still wanted to retain the staggered compression - this would allow the rear cylinder to still run lower compression. I ran the head data through the two stroke software to help me design a better head. I knew that if I could make the squish band useful I could gain additional performance from the motor. I still wanted to be able to run pump gas (89 octane would have to be acceptable since 92 is not available at all marina's). I found out that if I milled 1.1 mm from the surface of the head I would be able to achieve a maximum squish velocity (MSV) of 30 m/s on the front cylinder (a good number for a heavy watercraft). Though this is a vast improvement over the stock set up for the front cylinder, the rear cylinders squish thickness (about .40 mm thicker) would only get a marginal improvement (to about 22 m/s). But milling 1.1 mm from the head would remove some of the squish area from the front cylinder while it evens up the squish thickness difference a bit between the two cylinders. Some of it would have to be recut into it - but very little work would be needed. I would much rather have a properly designed squish band working for me than not. I would settle for opening up the dome of the front cylinder to make better use of this tub head design. After the material was milled I recut the squish area as needed. I touched up the rear cylinder to make it parallel to the piston crown and removed some material from the dome of the front cylinder since it was still a little bit too small. I ended up with squish thicknesses of 1.52 mm up front and 1.78 mm out back. This calculated out to a MSV of 29 m/s up front and 25 m/s for the rear. These are much better figures than the 16 m/s and 11 m/s it came with from Yamaha. The UCCR would end up being 13.65:1. That's a little over 10% higher than when I started - the numbers looked good.
 
After running the porting specs through some two stroke software it became very clear that the transfer port area was quite a bit too small. Without raising them I was able to increase the time/area by a significant amount. I changed the port roof angle from its "choked" angle to a design which has more area as well - much more flat top port roofs. This basic cylinder block has its ports cast the same as they were when it was a 701 cc motor - maybe even from when it was a 650 cc package. I also changed the vertical angle of the main and secondary port walls so they will release their charge a little more directly across the piston to help peak power. The match between the liner and the aluminum was terrible - I spent a great deal of time making it right. I also increased the exhaust port time/area by widening the port. I choose to make the port oval instead of giving it an unusual shape like we talked about this year. The 760 engine uses 84 mm pistons and its exhaust port has the same area as the 701 which uses 81 mm pistons. The additional bore size lets making the oval port shape much easier. It would have been even easier if I was going to raise the port as well but I didn't want to decrease the duration of the power stroke. I was able to achieve a good shape and time/area by widening the port to 64% of the bore. Though it weighed heavily on my mind (the thought of cutting the aluminum too thin) it turns out that there is plenty of material for this modification. I was able to increase the exhaust pipe entry port area too, though its shape is not as oval as the exhaust port or the aluminum immediately adjacent to it.
 
While working on the exhaust I discovered a 5 to 6 inch long crack in the aluminum casting of the inner wall in the rear most section of the pipe. I welded it to plug the water leak. I'm glad I decarboned the pipe or I may mot have seen it. When I measured the bores of the barrel I was surprised to find that they were still extremely round and measured exactly 84 mm - they needed only a fresh hone. The time meter showed 108 hours of use in the 2 years since I bought it - and much of that time has been spent towing multiple tubes with kids on them (I know I'm not supposed to do that). At the time I ordered replacement parts for this project I was unable to get the Pro-X cast pistons I wanted. I could not justify paying the amount of money Yamaha wanted for OEM replacement piston sets - literally 2 1/2 times more than after market, so I bought a set of Wiseco forged pistons for it. I did not get the XPS series (coated) pistons because I heard they had problems with shrinkage - collapsing of the thrust surfaces. The new Wiseco pistons came with .003" piston to wall clearance cut into them - what I call a perfect fit. The pistons I took out had .007" clearance. Additionally the new pistons are over 3 ounces lighter than the chunky Yamaha pieces.
 
Since the carburetors are of the down draft type and the intake makes a 90 degree bend into the crankcase, I added the Boyesen reed cage stuffer to the intake side. The stuffer has different sized passages (the horizontal divider is placed very low) to compensate for the mixture which wants to follow the contour of the intake manifold. It should prevent the mixture from slowing down there as well because the intake manifold opens up very large to allow it to feed the reed cage. I also topped of the carbs with a Pro-Tec K&N flame arrestor and velocity stacks which was left over from a Wave Raider project - I had to buy the larger adapter plates for use on the 44 mm carburetors.
 
In addition to the engine modifications I replaced the worn out stock impeller with the Solas I (eye) design - it is very close to the stock part as far as I could tell, and added a Rule 500 gph bilge pump to help keep the inside of the boat dry. If you haven't seen what cavitation can do to an impeller take a look at the photo I put up - click here.
 
The instructions that came with the Wiseco pistons said to add 2 ounces of oil per gallon of gas for the first tankful when used in oil injected motors. I thought that was a lot of oil to add to the already oil rich something-in-the-neighborhood-of 32:1 mixture it gets so I added only 16 ounces of oil to the 13 point something gallon fuel tank. I didn't like the thought of leaning out the fuel to air ratio by adding that much oil to the gas either. I left the low speed mixture screws alone but I opened the high speed mixture screws 1/2 turn. I did this to compensate for the additional exhaust area and head modifications. When it was done I started it up for a minute then let it cool off completely. I then performed a compression test using a Snap-On compression gauge. Up front the reading was 175 psi - the rear was showing 170 psi. This was an increase of 15 psi in both cylinders.
 
Last week I was able to take the craft out for its "run in." Immediately I noticed a deeper throatier sound. The throttle response seemed much more crisp than it was before. I planned to drive around the lake at different operating speeds until the first tank of gas was gone. I'm not one to baby a machine during any time in its life so I pretty much broke it in the way I drive it, with the exception of holding it at WOT - I would wait a bit for that. It was clear right away that the Wave Runner had a different personality - it would pop out of the water like a cork on steroids. That low octane sluggish feeling was gone.
 
My kids and my nephews and nieces were bugging me to take them tubing and I wasn't even through 5 gallons of gas yet. I told them it would have to wait a bit. I took my daughter Lauren for a ride - actually she drove while I observed. We pulled into an area with some tall grass and tree tops sticking out of the water to take a look at the fish that were in the water. Every few minutes we would start the boat to move to another spot, then we would shut it off and drift in so we wouldn't scare the fish. When we were going to leave the area I clicked the starter but the engine wouldn't start. I figured it was a fouled plug since I had done so many starts without really running the engine - perhaps it had become oil fouled. I jumped in the water and swam with the boat to push it to the shore as Lauren poked fun at me. I yanked the plugs out as she started building a sand castle to establish a home base. The spark plugs were the stainless steel Champions that my brother gave me last summer when we were at lake Havasu - they only had about an hour of riding time on them. Somehow I had forgotten to pack a couple of spares. It was kind of hot out so I wiped them off with a piece of paper and rested them on the hood - maybe they would dry off. While waiting Lauren started asking me the "what if's." What if we couldn't get off the island... What if we didn't have anything to eat... What if we had to stay there all day... What if we had to stay there all night!?!
 
It really wasn't an island, it was the shore of the lake. Though we were about 7 or 8 miles from camp we could walk there if we had to and I could see the marina from where I was standing. Lauren decided that she could remove and bend a nail from the nearby fence, attach it to a piece of string that she found and tie it all to a stick so she could catch us some fish for dinner. She would rub 2 sticks together to start a fire. She would spell out S.O.S. by using rocks on the beach so aircraft could see us and come to our rescue. I was asked what S.O.S. stood for - I really don't remember! I told her it meant "rescue us and we're not kidding!" I'll have to look that up (save our souls?!?). I wondered about the stick rubbing thing to start the fire and decided that if I could get any kind of spark from one of those Champions I could start a GREAT fire - we had gasoline! She had me thinking like a kid - the world's so big to kids. I looked over that fence she was going to take the nail out of - it was holding back cows! I never did like fresh water fish that much - I asked her how she felt about having a hamburger instead. She laughed and said "Oh yeah!" It seemed funny to me that there was no traffic on the lake right then. I remembered it was a Wednesday - not many people out during the middle of the week. It's not often we leave for a trip on a Tuesday, my clock was off. I put the plugs back in as I tried to sell her on the idea that the boat would now start. When it still wouldn't I knew I would have to replace them. Lauren started making more detailed plans and was clearly thinking about digging in for the long(er) haul.
 
After a few minutes I successfully flagged down a boat - the second one that drove by. I decided that I wasn't convincing enough when the first boat went by (it didn't stop) so I over compensated the hand and arm gestures to make sure the second boat stopped. Three guys in a blue boat pulled up. I told them I would like to give them money to go to the marina to buy me a set of plugs. The driver said that would be fine. I gave them one of the bad plugs so they could match it up and a ten dollar bill. I had a tow rope but I thought I could do 2 things at once this way. I could get new plugs and get to spend a few more minutes on the "island" with my daughter. We started using words like shipwrecked and marooned. I decided to name my GP760 the S.S. Minnow. We started singing the theme from Gilligans Island. Lauren asked me if I thought the guys we gave the money to would ever come back. I told her that since they stopped to help us there was a good chance they weren't going to run off with the $10 I gave them. I told her they would come back. If I wanted to walk about thirty feet I could have looked to see if their boat was at the marina. I wasn't worried, I figured sooner or later my brother would cruise by riding his XL1200 anyway. His son Jason would probably be with him on a Wave Raider. We had lots of daylight left.
 
It seemed like it took longer than it should have to drive the 1/2 mile to the dock, run in and grab a couple of plugs and come back. Lauren asked me again if those guys looked like they could be trusted. Before I could answer, I saw them coming closer. One of the passengers in the boat handed me the new plugs and the change (about 30 cents). I thanked them for the assistance as offered to buy them some beers if they cared to stick around long enough for me to screw in the plugs and get started. The driver smiled and suddenly looked real thirsty. It occurred to me that he could probably put away some serious beer. The Wave Runner took a few seconds of full choke to start. I thought that was a little curious because it was about 85 degrees outside - it never takes choke on warm days. I only had $22 dollars left on me and I (now) wanted to get a spare set of plugs too, but I could make another trip for them if the beer was really expensive at the marina. It was expensive - the 2 plugs were $9 something (what a rip) and the beer took just about the rest of the money I had. I didn't really care because we were going home! It turns out that out rescuers were our neighbors and were parked about 4 or 5 campers more inland than we were.
 
I later found out that the plugs were not fouled after all. The reason the motor would not start after we were done looking at the fish was because it needed choke. I did not think it needed it (actually I thought it was oil or perhaps fuel fouled) so I never pulled the knob. I later turned out the low speed mixture screws (1/6 of a turn) and my starting problems went away. I should have considered that I would be running a bit leaner at low speed too and richened up that circuit before I started as well. When I had the spark plugs out (on the island) with the sun fully shining on the lathe cut piston crowns I could see the burn pattern real well. Things looked good inside the motor - I was getting happy.
 
I poured some more 89 octane gas into the tank and headed out for another ride. I had run about 1 full tank through the motor so I was thinking it would be a good time to see what it had on top. With the water as smooth as I've seen it on that lake the speedometer (actually a ballpark guesser to the tune of several miles per hour I'm told) showed 62 MPH. That's 2 MPH higher than I've ever seen it register - 60 was my previous best and I only saw it one time. Most of the time it used to read 55 or 56 as a top speed on smooth water and about 49 or 50 in rougher water. The natural, part throttle cruise speed the stock motor liked was about 45. At that speed the motor would turn about 5500 RPM. Maximum RPM is limited at about 6700 according to the tach. It now became clear that not only was the motor able to take off with much more authority it actually had some speed left when the tach showed 6000 RPM. It used to be useless to turn it higher than that because the speed would not increase. Another thing that became clear was that its natural part throttle cruise speed was now up to about 52 - quite a difference. I never saw 62 again last week but I never had flat water like that again either. I saw a lot of 58's and 59's and several 60's. It would be difficult to say that the top speed was not improved - because I'm sure it is up a couple mph's. When I entered the stock engines parameters including port time area and output figures into the 2 stroke software and compared it to the new port time areas using the same BMEP, the data shows power to now be 102 HP @ 6300 an increase of 12 HP at the same RPM.
 
I spent some time trying to figure it all out but I think it would be safe to say from my experience that it indeed is possible to increase low speed power and midrange and peak speed as well when modifying (at least) this model of personal watercraft. When towing the tubes full of kids the boat planes them (and me) instantly. There's a little thing that kids like to do to see if you're paying attention while cruising in the no wake zone or just before you get to it - they submarine the tubes. Doing this exposes the inner circle of the covered tube to the water and the center section starts to fill up with water, creating a huge drag on the tow vehicle. When they do it, it usually stops my forward progress - it's like a couple of parachutes have been opened, or like a couple of anchors have been dropped. When I'm not paying attention it can catch me off guard in such a way that I almost tip over. Real funny to the kids. When I see them doing it sometimes I'll gas it real quick to see if I can knock them off their tube - catch them off balance. Unfortunately there is so much drag against the water that even when I pulled the throttle all the way in it would prevent much forward movement. Kind of like a stall in an airplane - the motors running but there's no progress. I am happy to say that this situation has been rectified. I know some kids who can attest to this by telling of how much water they drank and how long they coughed after I pulled the trigger last week when they were doing their little antics. This boat now has enough power to keep pulling the submarined tubes under water until the tube passengers have to let go because of fear of being deep under water - heh. I doubt this boat will win any drag races against 1100's or 1200's but that wasn't my intention with this project anyway - this was what I call routine maintenance. It occurred to me that my gas mileage seemed to be better as well - though I've got no hard data about this. I had no trouble burning 40 gallons of fuel in the 5 days on the water. With watercraft fuel mileage is a funny thing. The power delivery is so inefficient (talk about slippage) it's a wonder they do as well as they do. I'm sure my wallet will let me know.
 
Rick

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Date Last Modified: 6/23/99
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